Location DataHistoryPerforationsStimulationsProduction RecordsUIC DataProduction TestsInspection Data
03-073-11536-00-00 | Date Permit Issued | 01-12-2016 | Form: 2 | original |
03-073-11536-00-00 | Date Well Spudded | 01-15-2016 | TRK |
03-073-11536-00-00 | Date Commenced | 01-16-2016 | |
03-073-11536-00-00 | Completion Type | 07-22-2016 | Controlled Production |
03-073-11536-00-00 | Date Completed | 07-22-2016 | |
03-073-11536-00-00 | Wellbore Status | 07-22-2016 | Active |
03-073-11536-00-00 | First Production | 09-06-2016 | |
03-073-11536-00-00 | Well Status | 09-06-2016 | PR |
03-073-11536-00-00 | Change of Operator | 01-18-2022 | Operator changed from 197, TMR Exploration, Inc to 1630, Williamson Pumping Service, Inc |
03-073-11536-00-00 | Deviation Type | 05-19-2024 | Vertical |
03-073-11536-00-00 | Operator | 05-19-2024 | 1630 |
03-073-11536-00-00 | Well Name | 05-19-2024 | Powers 7 |
03-073-11536-00-00 | Well Number | 05-19-2024 | 1 |
03-073-11536-00-00 | Well Type | 05-19-2024 | OIL |
03-073-11536-00-00 | Wellbore Type | 05-19-2024 | Oil - Production |
48011 | 03-073-11536-00-00 | 2740 | 2743 | 07-22-2016 | | | | BUCKRANGE | |
No UIC data records available |
09-06-2016
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Gas Well Backflow Pressure Test
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0
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09-06-2016
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Production Test
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P
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24
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12.0000
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12.0000
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28.0000
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O
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temp allowable
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